[1]Limits for Harmonic Current Emissions (Equipment Input Current < 16A Per Phase), IEC/EN 61000-3-2, 1995.
[2]B. Wilkenson, “Power Factor Correction and IEC 555-2,” Power Techniques Magazine, pp. 20-24, 1991.
[3]Mohan. U. R/原著,江炫樟/編輯,電力電子學,第三版,全華圖書股份有限公司,2008年。
[4]N. Mohan, T. M. Undeland, and W. P. Robbins, Power Electronics: Converters, Applications, and Design, Third Edition, John Wiley &; Sons, Inc., 2003.
[5]S. S. Kim and P. N. Enjeti, “A modular single-phase power factor correction scheme with a harmonic filtering function,” IEEE Transactions on Industrial Electronics, vol. 50, no. 2, pp. 328-335, April 2003.
[6]許元豪,「徹底剖析工作於連續導通模式下升壓型PFC 線路中高壓快速恢復二極管所導致的五種功率損耗模式」,電子月刊,2008年2月。[7]J. Luo, “New PFC solution for the future ICE1PCS01/02,” Infineon Power Seminar, 16th Sept. 2004, Singapore.
[8]張厚升,「功率因數(PFC)校正技術的新型控制技術的優缺點對比」,電源世界,2007年9月。
[9]洪瑞鴻,「2kW功率因數修正器研製」,國立台灣科技大學電子工程系研究所碩士論文,民國94年。[10]L. Huber, L. Gang, and M. M. Jovanovic, “Design-oriented analysis and performance evaluation of buck PFC front-end,” IEEE Transactions on Industrial Electronics, vol. 25, no. 1, pp. 85-94, May 2010.
[11]張家榮 ,「不需輸入電壓感測之主動型功因修正 AC/DC 轉換器的研製」,國立中山大學電機工程系研究所碩士論文,民國95年。[12]C. A. Canesin and I. Barbi, “Analysis and design of constant-frequency peak-current-controlled high-power-factor boost rectifier with slope compensation,” in Proc. IEEE APEC '96, vol. 2, pp. 807-813, March 1996.
[13]Texas Instruments Incorporated, “UC3854 high power factor preregulator,” Datasheet, 1999.
[14]M. F. Schlecht and B. A. Miwa, “Active power factor correction for switching power supplies,” IEEE Transactions on Power Electronics, vol. 1, no. 4, Oct. 1987.
[15]ST Microelectronics, “L6561, enhanced transition mode power factor corrector,” Application Note AN966, 2003.
[16]ST Microelectronics, “EVAL6562-375W evaluation board L6562-based 375W FOT-controlled PFC pre-regulator,” Application Note AN1895, 2004.
[17]ST Microelectronics, “Solution for designing a 400 W fixed off-time controlled PFC pre-regulator with the L6562A,” Application Note AN2782, 2010.
[18]ST Microelectronics, “Design of fixed-off-time-controllered PFC pre-regulators with the L6562,” Application Note AN1792, 2003.
[19]R. B. Ridley, “A new continuous-time model for current-mode control with constant frequency, constant on-time and constant off-time, in CCM and DCM,” IEEE Power Electronics Specialists Conference Record, San Antonio, Texas, pp. 382-389, 1990.
[20]C. Adragna, S. De Simone, and G. Gattavari, “New fixed off-time PWM modulator provides constant frequency operation in boost PFC pre-regulators,” in Proc. IEEE SPEEDAM, pp. 656-661, 2008.
[21]ST Microelectronics, “400 W FOT-controlled PFC pre-regulator with the L6563S,” Application Note AN2994. 2010.
[22]Texas Instruments Inc., “UCC29910 buck PFC controller,” Datasheet, June 2010.
[23]ST Microelectronics, “L6561, power factor corrector,” Datasheet, 2003.
[24]林建宇,「雙模式升壓型功率因數修正器最佳化設計」,國立台灣科技大學電子工程系研究所碩士論文,民國99年。[25]謝沐田,高低頻變壓器設計,全華科技圖書股份有限公司,2005年11月。
[26]TDK Ferrite Cores for Power Supply and EMI/RFI Filter, 2007.
[27]ON Semiconductor, “Power factor correction stages operating in critical conduction mode,” Application Note AND8123/D, 2003.
[28]X. Wu, J. Yang, J. Zhang, and M. Xu, “Design considerations of soft-switched buck PFC converter with constant on-time (COT) control,” IEEE Transactions on Power Electronics, vol. 26, no. 11, pp. 3144-3151, Nov. 2011.
[29]Texas Instruments Inc., “Power factor correction using the buck topology-efficiency benefits and practical design considerations,” Application Note SLUP264, June 2010.
[30]張家鏵,「GaN FET應用於高頻化錯相式降壓型功率因數修正器之研製」,國立台灣科技大學電子工程系研究所碩士論文,民國102年。[31]R. W. Erickson, D. Maksimovic, Fundamentals of Power Electronics, 2nd Edition, 2000.
[32]C. P. Basso, “Switch-mode power supplies, SPICE simulations and practial designs, ” 1st Edition, 2008.
[33]SHINDENGEN, “Super fast recovery rectifiers,” Shindengen Electric Mfg. Co. Ltd., 2000.
[34]SHINDENGEN, “Low forward voltage low noise type single In-line package,” Shindengen Electric Mfg. Co. Ltd., 2010.
[35]陳彥捷,「雙模式控制返馳式轉換器最佳化設計」,國立台灣科技大學電子工程系研究所碩士論文,民國100年。